Yaskawa U1000 iQpump Drive Fault Codes:
| Fault Code and Meaning | Cause and Remedy |
|---|---|
| ACCUM Accum Level Accumulated Level Fault: The total volume of water flow measured over time by the flow meter has exceeded the fault level setting. | Cause: The accumulated level has exceeded the values set in P6-11 to P6-14. This is only effective when P6-15 (Accumulated Behavior) is set to 2 (fault with manual monitor reset) or 3 (fault with automatic monitor reset). Remedy:
|
| AJF Anti-Jam Fault Anti-Jam Fault | Cause: The drive was not able to clear debris from the impeller in fewer than the number of attempts set in P7-02. This is only effective when P7-01, Anti-jam Operation is set to 1 (enabled). Remedy:
|
| Aov Power Supply Overvoltage The input power supply voltage became equal to or higher than the Input Power Supply Overvoltage Detection Level. 200 V Class: approx 277 Vrms 400 V Class: approx 630 Vrms | Cause: The power supply voltage exceeded the range listed in drive input power specifications, regenerative operation was performed when capacity was too small, or the power supply circuit opened during regeneration. Remedy:
|
| AUv Power Supply Undervoltage The input power supply voltage became equal to or lower than the Input Power Supply Undervoltage Detection Level (L2-21). | Cause: The capacity of the power supply is too small, distortion is too large, a phase loss occurred, or the built-in fuse is open (internal transistor destroyed). Remedy:
|
| AUXFB PI Aux Lvl Loss Wire-break detection for PI Aux Feedback Level | Cause: The analog input programmed for “PI Aux FB Level” has dropped below 3 mA or risen above 21 mA for longer than 1 second. Remedy:
|
| bAT Keypad Battery Voltage Low | Cause: The keypad battery is low. Remedy:
|
| boL Braking Transistor Overload Fault The braking transistor reached its overload level. | Cause: The wrong braking resistor is installed. Remedy:
|
| bUS Option Communication Error Connection lost after establishing communication or detected when run command frequency reference is assigned to option card. | Cause: No signal from PLC, faulty communications wiring, existing short circuit, noise, or damaged option card. Remedy:
|
| CE MEMOBUS/Modbus Communication Error Control data was not received for the CE detection time set to H5-09. | Cause: Faulty communications wiring, existing short circuit, or communication data error due to noise. Remedy:
|
| CF Control Fault Torque limit reached continuously for 3 seconds after Stop command in OLV Control. | Cause: Motor parameters set improperly, torque limit too low, or load inertia is too big. Remedy:
|
| CoF Current Offset Fault Drive starts operation while current-detection circuit failure or induced voltage remains in motor. | Cause: The drive performed a current offset adjustment while the motor was rotating, or hardware problem. Remedy:
|
| CPF00 to CPF45 Control Circuit Error (Includes CPF00-CPF03, CPF07-08, CPF11-14, CPF16-24, CPF26-35, CPF40-45) | Cause: Hardware is damaged or connector on the keypad is damaged. Remedy:
|
| CPF06 EEPROM Memory Data Error Error in the data saved to EEPROM. | Cause: There is an error in EEPROM control circuit or power supply was switched off while parameters were being saved. Remedy:
|
| CPF25 Terminal Board Not Connected | Cause: Terminal board is not connected correctly. Remedy:
|
| DIFF Differential Det Differential Feedback Detected | Cause: The difference between the PID Feedback and the Differential Feedback exceeded the P4-18 level for the time set in P4-19. Remedy:
|
| doH Damping Resistor Overheat Temperature of built-in damping resistor exceeded set value. | Cause: Power supply capacity too small, distortion too large, or phase loss occurred. Remedy:
|
| E5 SI-T3 Watchdog Timer Error The watchdog timed out. | Cause: Data has not been received from the PLC. Remedy:
|
| EF0 Option Card External Fault An external fault condition is present. | Cause: An external fault was received from the PLC and F6-03 is not 3, or problem with PLC program. Remedy:
|
| EF1 to EF8 Pump Fault (Input Terminals S1-S8) External fault at multi-function input terminal. | Cause: An external device tripped an alarm function, wiring is incorrect, or multi-function contact input setting is incorrect. Remedy:
|
| Err EEPROM Write Error Data cannot be written to the EEPROM. | Cause: Noise corrupted data while writing, or hardware problem. Remedy:
|
| FAn Internal Fan Fault Fan or magnetic contactor failure. | Cause: Internal cooling fan malfunctioned, or fault detected in internal cooling fan or magnetic contactor to power supply. Remedy:
|
| FbL PID Feedback Loss PID feedback level is below detection level set to b5-13. | Cause: Parameters set inappropriately, incorrect PID feedback wiring, or problem with feedback sensor. Remedy:
|
| FDBKL Wire Break PID Feedback Loss Analog input programmed for PID feedback has risen above 21 mA or fallen below 3 mA. | Cause: The analog input programmed for PID feedback loss has risen above 21 mA or fallen below 3 mA. Remedy:
|
| Fdv Power Supply Frequency Fault Input power supply frequency exceeded allowable fluctuation. | Cause: Momentary power loss, loose wiring, large voltage fluctuation, or built-in fuse open. Remedy:
|
| GF Ground Fault A current short to ground exceeded 50% of rated current on the output side of the drive. | Cause: Motor insulation is damaged; A damaged motor cable is creating a short circuit; Excessive leakage current at drive output; Hardware problem. Remedy:
|
| HFB High Feedback | Cause: The feedback signal is too high (risen above level set in P1-11 for time set in P1-12). Remedy:
|
| HIAUX High PI Auxiliary Feedback Level | Cause: PI Aux Feedback has risen above the Q6-12 level for longer than Q6-13 time. Remedy:
|
| HIFLO High Flow | Cause: The meter has detected a high flow condition (risen above P6-17 level for time set in P6-18). Remedy:
|
| HISUC High Suction Pressure | Cause: The suction pressure has fallen below the level set in Q5-12 for longer than the time set in Q5-13. Remedy:
|
| HWL High Water Level | Cause: The “High Water Level” digital input is active (H1-xx = 90); Low Water Level switch activated or P1-31 programmed incorrectly. Remedy:
|
| LF Output Phase Loss | Cause: Output cable disconnected; Motor winding damaged; Output terminal loose; Rated current of motor is less than 5% of drive rated current; Output transistor damaged. Remedy:
|
| LFB Low Feedback | Cause: The feedback signal is too low (dropped below P1-08 for time set in P1-09). Remedy:
|
| LF2 Output Current Imbalance | Cause: One or more phases in output current lost; Phase loss on output side; Loose terminal wires; Output circuit damaged; Motor impedance uneven. Remedy:
|
| LOAUX Low PI Auxiliary Feedback Level | Cause: PI Aux Feedback has fallen below Q6-09 level for longer than time set in Q6-10. Remedy:
|
| LOP Loss of Prime | Cause: Pump load (current/power) dropped below P1-19 level for time set in P1-20. Remedy:
|
| LOSUC Low Suction Pressure | Cause: Suction pressure has fallen below Q5-09 level for longer than time set in Q5-10. Remedy:
|
| LOWFL Low Flow | Cause: Insufficient flow; Measured flow fallen below P6-06 level for time set in P6-07. Remedy:
|
| LOWWL Low Water Level | Cause: Water level fallen below level set in Q4-09 for longer than time set in Q4-10. Remedy:
|
| LWL Low Water Level (Digital Input) | Cause: The “Low Water Level” digital input is active; Switch defective or P1-30 programmed incorrectly. Remedy:
|
| NMS Not Maintaining Setpoint | Cause: Feedback deviates from setpoint > P1-15 for time set in P1-16; Setpoint cannot be maintained. Remedy:
|
| nSE Node Setup Error | Cause: A terminal assigned to the node setup function closed during run; Run command issued while node setup active. Remedy:
|
| oC Overcurrent | Cause: Drive sensors detected output current greater than specified level. Causes include: damaged motor/insulation, shorted cables, load too heavy, accel/decel too short, specialized motor usage, V/f setting issues, excessive torque compensation. Remedy:
|
| oFA00 Option Card Connection Error at Option Port CN5-A | Cause: The option card installed into port CN5-A is incompatible with the drive. Remedy:
|
| oFA01 Option Card Fault at Option Port CN5-A | Cause: The option card connection to port CN5-A is faulty. Remedy:
|
| oFA03 to oFA06 oFA10, oFA11 oFA12 to oFA17 oFA30 to oFA43 Option Card Error (CN5-A) | Cause: Option card or hardware is damaged. Remedy:
|
| oFb00 Option Card Fault at Option Port CN5-B (Compatibility) | Cause: 1. Option card in CN5-B is incompatible. 2. A communication option card has been installed in CN5-B. Remedy:
|
| oFb01 Option Card Fault at Option Port CN5-B (Connection) | Cause: The option card connection to port CN5-B is faulty. Remedy:
|
| oFb02 Option Card Fault at Option Port CN5-B (Duplicate Type) | Cause: An option card of the same type is already installed in option port CN5-A. Remedy:
|
| oFb03 to oFb11 oFb12 to oFb17 Option card error at Option Port CN5-B | Cause: Option card or hardware is damaged. Remedy:
|
| oFC00 Option Card Connection Error at Option Port CN5-C | Cause: 1. Option card in CN5-C is incompatible. 2. A communication option card is installed in CN5-C. Remedy:
|
| oFC01 Option Card Fault at Option Port CN5-C (Connection) | Cause: The option card connection to port CN5-C is faulty. Remedy:
|
| oFC02 Option Card Fault at Option Port CN5-C (Duplicate Type) | Cause: An option card of the same type is already installed in CN5-A or CN5-B. Remedy:
|
| oFC03 to oFC11 oFC12 to oFC17 Option Card Error at Option Port CN5-C | Cause: Option card or hardware is damaged. Remedy:
|
| oFC50 to oFC55 Option Card Error at Option Port CN5-C | Cause: Option card or hardware is damaged. Remedy:
|
| oH Heatsink Overheat | Cause: Heatsink temperature exceeded the pre-alarm level (L8-02). Surrounding temp too high or Load too heavy. Remedy:
|
| Internal cooling fan is stopped | Cause: Cooling fan failure or end of life. Remedy:
|
| oH1 Overheat 1 (Heatsink Overheat) | Cause: Heatsink temperature exceeded the drive overheat level. Remedy:
|
| oH3 Motor Overheat Alarm (PTC Input) | Cause: Motor has overheated. Signal at A1, A2, or A3 exceeded fault detection level. Remedy:
|
| oH4 Motor Overheat Fault (PTC Input) | Cause: Motor has overheated (Fault level exceeded). Remedy:
|
| oL1 Motor Overload | Cause: Electronic motor overload protection tripped. Load too heavy or cycle times too short. Remedy:
|
| oL2 Drive Overload | Cause: The thermal sensor of the drive triggered overload protection. Remedy:
|
| oL3 Overtorque Detection 1 | Cause: Current exceeded value in L6-02 for longer than time in L6-03. Remedy:
|
| oL4 Overtorque Detection 2 | Cause: Current exceeded value in L6-05 for longer than time in L6-06. Remedy:
|
| oPr External HOA Keypad Connection Fault | Cause: The HOA keypad has been disconnected from the drive. Remedy:
|
| ov Control Circuit Overvoltage | Cause: Voltage in control circuit exceeded level (approx 450V for 200V class / 900V for 400V class). Remedy:
|
| PoC Pump Over Cycle | Cause: Pump exceeded cycle count (P2-10) within time (P2-11). Remedy:
|
| SCF Safety Circuit Fault | Cause: The safety circuit is damaged. Remedy:
|
| SEr Too Many Speed Search Restarts | Cause: Parameters related to Speed Search are set to the wrong values. Remedy:
|
| SoH Snubber Discharge Resistor Overheat | Cause:
Remedy:
|
| SPL Suction Pressure Loss | Cause: An analog input programmed for setting 23 “WaterLvl/Suction” has dropped below 3 mA or risen above 21 mA for longer than 1 second. Remedy:
|
| SrC Phase Order Detection Fault | Cause:
Remedy:
|
| Srr Internal Resistance Fault | Cause: The snubber discharge resistor or peripheral circuits failed. Remedy:
|
| TdE Time Data Error | Cause: An error has occurred in the Real-Clock Time function of the HOA keypad. Remedy:
|
| TIE Time Interval Error | Cause: An error has occurred in the Real-Time Clock function of the HOA keypad. Remedy:
|
| TIM Time Not Set | Cause: The Real-Time Clock for the HOA keypad is not set in parameter o4-17 (drive is new, o4-17 was reset, or battery is low/replaced). Remedy:
|
| UL3 Undertorque Detection 1 | Cause:
Remedy:
|
| UL4 Undertorque Detection 2 | Cause:
Remedy:
|
| UL6 Motor Underload | Cause: The output current has fallen below the motor underload curve defined in L6-14 for longer than the time set to L6-03. Remedy:
|
| Uv1 Control Circuit Undervoltage Fault | Cause:
Remedy:
|
| Uv2 Control Power Supply Voltage Fault | Cause:
Remedy:
|
| Uv3 Undervoltage 3 (Soft-Charge Bypass Circuit Fault) | Cause: The relay or contactor on the soft-charge bypass circuit is damaged. Remedy:
|
| VLTS Volute-Thermostat Fault | Cause:
Remedy:
|
| WLL Water Level Loss | Cause: An analog input programmed for setting 23 “WaterLvl/Suction” has dropped below 3 mA or risen above 21 mA for longer than 1 second. Remedy:
|
| ACCUM Accumulated Level Error | Cause: The accumulated level has exceeded the values set in P6-11 to P6-14. This is only effective when P6-15 (Accumulated Behavior) is set to 1 (alarm). Remedy:
|
| Accum Lvl Reached Flow Accumulation level reached | Cause: Accum Behavior P6-15 is set to 5 (Stop, Alarm, & Reset) and the Accumulated Level has been reached. Remedy:
|
| AEr Station Address Setting Error | Cause: Station number is set outside the possible setting range (CC-Link, CANopen, MECHATROLINK). Remedy:
|
| Anti-Jam Active Anti-Jam Alarm | Cause: The drive was not able to clear debris from the impeller in fewer than the attempts set in P7-02. (Effective when P7-01 is enabled). Remedy:
|
| AUv Power Supply Undervoltage | Cause: The power supply voltage is low or a phase loss occurred in the input power supply. Remedy:
|
| AUXFB PI Aux Lvl Loss (Wire-break detection) | Cause: The analog input programmed for “PI Aux FB Level” (H3-XX = 27) has dropped below 3 mA or risen above 21 mA for longer than 1 second. Remedy:
|
| Backup FdBk Lost Backup Feedback Device lost | Cause: Wire-break on Analog Input Terminal (H3-XX = 24) or Backup PI Feedback Transducer is broken. Remedy:
|
| bAT Keypad Battery Voltage Low | Cause: The keypad battery is low. Remedy:
|
| bb Baseblock | Cause: External baseblock signal was entered via one of the multi-function input terminals (S1 to S8). Remedy:
|
| boL Braking Transistor Overload Fault | Cause: The proper braking resistor has not been installed. Remedy:
|
| bUS Option Communication Error | Cause: Connection broken, master controller stopped, option damaged, or data error due to noise. Remedy:
|
| CALL Serial Communication Transmission Error | Cause: Communication not established due to wiring faults, programming errors, damaged circuitry, or incorrect termination. Remedy:
|
| CE MEMOBUS/Modbus Communication Error | Cause: Data error due to noise, incompatible protocol, CE detection time (H5-09) too short, or cable damage. Remedy:
|
| CE (Run at H5-14) Comm Loss Run at H5-14 | Cause: Similar to standard CE fault (Noise, Protocol incompatibility, Timing, or Cable issues) but drive continues to run based on settings. Remedy:
|
| CrST Cannot Reset | Cause: Fault reset was being executed when a Run command was entered. Remedy:
|
| Current Limit Foldback Current Limit Foldback | Cause: Drive output speed is being limited due to the output current limit. Remedy:
|
| CyC MECHATROLINK Comm. Cycle Setting Error | Cause: The controller is using a comm. cycle beyond the allowable setting range. Remedy:
|
| De-Scale/De-rag Active De-scale is running | Cause: De-scale is programmed and enough run time has been accumulated. Remedy:
|
| Differential FB Detected Differential Feedback Detected | Cause: The difference between the PID Feedback and the Differential Feedback exceeded P4-18 level for time set in P4-19. Remedy:
|
| dnE Drive Disabled | Cause: “Drive Enable” is set to a multi-function contact input (H1-XX = 6A) and the contact is open. Remedy:
|
| doH Damping Resistor Overheat | Cause: Power supply capacity too small, distortion too large, or phase loss in input power. Remedy:
|
| EF Forward/Reverse Run Command Input Error | Cause: Both forward run and reverse run closed simultaneously for longer than 0.5 s. Remedy:
|
| EF0 Option Card External Fault | Cause: An external fault was received from the PLC, or there is a problem with the PLC program. Remedy:
|
| EF1 to EF8 Pump Fault (Input Terminals S1-S8) | Cause: An external device tripped an alarm, wiring is incorrect, or multi-function inputs are set incorrectly. Remedy:
|
| FAn Internal Fan Error | Cause: Internal cooling fan has malfunctioned or fault detected in the magnetic contactor. Remedy:
|
| Fdv Power Supply Frequency Fault | Cause: The input power supply frequency exceeded the allowable frequency fluctuation.
Remedy:
|
| Feedback Loss Go To Freq. b5-13 PI Feedback Loss | Cause: PI feedback source is incorrectly installed or is not working. Effective only when b5-12 is set to 3 (Run at b5-13). Remedy:
|
| Feedback Loss Wire Break PI Feedback Loss | Cause: PI feedback source is incorrectly installed or is not working (Analog input > 21 mA or < 3 mA). Effective when b5-12 is set to 1. Remedy:
|
| Freq. Ref Pump Min (P1-06) Minimum Pump Frequency Reference | Cause: The frequency reference is set lower than P1-06 while the drive is NOT in PI Mode and Minimum Pump Frequency is enabled. Remedy:
|
| Freq. Ref Thrust (P4-12) Thrust Frequency Reference | Cause: The frequency reference is set lower than P4-12 while the drive is NOT in PI Mode and Thrust bearing is enabled. Remedy:
|
| Hbb Safe Disable Signal Input (Both Channels Open) | Cause:
Remedy:
|
| HbbF Safe Disable Signal Input (One Channel Open) | Cause:
Remedy:
|
| HCA Current Alarm | Cause: Drive current exceeded overcurrent warning level (150% of rated current).
Remedy:
|
| HIAUX High PI Auxiliary Feedback Level | Cause: PI Aux Feedback risen above Q6-12 level for time set in Q6-13 (Drive in AUTO). Remedy:
|
| HIFLO High Flow Error | Cause: The flow is too high / Meter detected high flow condition. Remedy:
|
| High Feedback High FB Sensed High Feedback Level Alarm | Cause: The feedback signal is too high (above P1-11 level). Remedy:
|
| HISUC High Section Pressure | Cause: Suction pressure has fallen below level in Q5-12 (Note: Alarm name says High, Description discusses falling below level – logic per manual). Remedy:
|
| LOAUX Low PI Auxiliary Feedback Level | Cause: PI Aux Feedback fallen below Q6-09 level for time set in Q6-10 (HAND or AUTO). Remedy:
|
| LOP Loss of Prime | Cause: Measured water quantity dropped below P1-19 level for time P1-20. (Dry well, air in system, no water). Remedy:
|
| LOSUC Low Section Pressure | Cause: Suction pressure fallen below level Q5-09 for time Q5-10. Remedy:
|
| Low City Pressure Low City Pressure | Cause: Insufficient pressure on inlet to pump (Input P4-24/P4-21 active). Remedy:
|
| Low Feedback Low FB Sensed Low Feedback Level Alarm | Cause: The feedback signal is too low (dropped below P1-08). Remedy:
|
| LOWFL Low Flow | Cause: Insufficient flow (measured water flow below P6-06 for time P6-07). Remedy:
|
| Low Suction Pressure Low Suction Pressure | Cause: Insufficient suction pressure present (Digital input activated). Remedy:
|
| Low Water in Tank Low Water in Tank | Cause: Insufficient pressure on inlet (Low water level input activated). Remedy:
|
| LOWWL Low Water Level | Cause: Water level fallen below Q4-09 level for time Q4-10. Remedy:
|
| LT-1 Cooling Fan Maintenance Time | Cause: The cooling fan has reached 90% of its expected performance life. Remedy:
|
| LT-2 Capacitor Maintenance Time | Cause: Main circuit and control circuit capacitors have reached 90% of expected performance lives. Remedy:
|
| LT-3 Soft Charge Bypass Relay Maintenance Time | Cause: DC bus soft charge relay has reached 90% of expected performance life. Remedy:
|
| LT-4 IGBT Maintenance Time (50%) | Cause: IGBTs have reached 50% of their expected performance life. Remedy:
|
| Main FdBk Lost Using Backup FB Main Feedback Device Lost | Cause:
Remedy:
|
| NMS Not Maintaining Setpoint | Cause: Feedback deviates from setpoint > P1-15 for time P1-16 (P1-17 set to 1). Remedy:
|
| oH Heatsink Overheat | Cause: Heatsink temperature exceeded L8-02 level.
Remedy:
|
| oH2 Drive Overheat Warning | Cause: “Drive Overheat Warning” was input to a multi-function input terminal, S1 through S8 (H1-xx= B). An external device triggered an overheat warning in the drive. Remedy:
|
| oH3 Motor Overheat | Cause: The motor overheat signal entered to a multi-function analog input terminal exceeded the alarm level. Common causes include:
Remedy:
|
| oL1 Motor Overload | Cause: The electronic motor overload protection tripped. Possible causes:
Remedy:
|
| oL2 Drive Overload | Cause: The thermal sensor of the drive triggered overload protection. Possible causes:
Remedy:
|
| oL3 Overtorque Detection 1 | Cause: The current has exceeded the value set for torque detection (L6-02) for longer than the allowable time (L6-03).
Remedy:
|
| oL4 Overtorque Detection 2 | Cause: The current has exceeded the value set for Overtorque Detection 2 (L6-05) for longer than the allowable time (L6-06). Remedy:
|
| ov Control Circuit Overvoltage | Cause: Voltage in the control circuit has exceeded the overvoltage level (approx 450V for 200V class; 900V for 400V class).
Remedy:
|
| N/A (MC Chat) Magnetic Contactor Chattering | Cause: Chattering in the magnetic contactor (MC) installed between the drive output terminals and the motor. Remedy:
|
| N/A (Phase) Input Power Phase Loss | Cause: There is a phase loss or an imbalance in the interphase voltages of the input power supply. Remedy:
|
| PoC Pump Over Cycle | Cause: The pump has exceeded the number of cycles set in P2-10 in the time set in P2-11. Remedy:
|
| R-DNE-S[] Remote Drive Disable | Cause: Terminal S[] has been closed (or open depending on setting) for the time set in P4-26. Remedy:
|
| SE MEMOBUS/Modbus Test Mode Error | Cause: A digital input set to 67H (MEMOBUS/Modbus test) was closed while the drive was running. Remedy:
|
| SPL Suction Pressure Loss | Cause: Wire-break detection for suction pressure. An analog input programmed for setting 23 has dropped below 3mA or risen above 21mA. Remedy:
|
| SrC Phase Order Detection Fault | Cause: The phase rotation direction for the input power supply changed.
Remedy:
|
| UL3 Undertorque Detection 1 | Cause: The current has fallen below the minimum value set for torque detection (L6-02) for longer than the allowable time (L6-03).
Remedy:
|
| UL4 Undertorque Detection 2 | Cause: The current has fallen below the minimum value set for torque detection (L6-05) for longer than the allowable time (L6-06). Remedy:
|
| UL6 Motor Underload | Cause: The load has fallen below the underload curve defined in L6-14. Remedy:
|
| Uv Control Circuit Undervoltage | Cause:
Remedy:
|
| WLL Water Level Loss | Cause: An analog input programmed for setting 23 “WaterLvl/Suction” has dropped below 3 mA or risen above 21 mA for longer than 1 second. Remedy:
|
| oPE01 Drive Capacity Setting Fault | Cause: The drive model selection (o2-04) and the actual capacity of the drive are not the same. Remedy: Correct the value set to o2-04 so it matches the drive capacity. |
| oPE02 Parameter Range Setting Error | Cause: Parameters were set outside the possible setting range. Remedy:
|
| oPE03 Multi-Function Input Selection Error | Cause: A contradictory setting is assigned to multi-function contact inputs H1-01 to H1-08. Examples include:
Remedy:
|
| oPE04 Initialization Required (Term <-> Ctrl Chg) | Cause: The drive, control board, or terminal board have been replaced and the parameter settings between the control board and the terminal board no longer match. Remedy:
|
| oPE05 Run Command/Frequency Reference Source Selection Error | Cause:
Remedy:
|
| oPE07 Multi-Function Analog Input Selection Error | Cause: A contradictory setting is assigned to multi-function analog inputs H3-02, H3-10, or H3-06, or PID functions conflict.
Remedy:
|
| oPE08 Parameter Range Setting Error | Cause: Parameters were set outside the possible setting range. Remedy:
|
| oPE09 PID Control Selection Fault | Cause: PID control function selection is incorrect (requires b5-01 = 1 to 4).
Remedy:
|
| oPE10 V/f Data Setting Error | Cause: V/f pattern setting error. One of the following errors occurred: E1-09 ≤ E1-07 < E1-06 ≤ E1-11 ≤ E1-04. Remedy: Correct the settings for E1-04, E1-06, E1-07, E1-09, and E1-11 to follow the required hierarchy. |
| oPE11 Carrier Frequency Setting Error | Cause: The following contradictory settings occurred:
Remedy: Correct the setting for the carrier frequency parameters. |
| oPE18 Online Tuning Parameter Setting Error | Cause: One of the following errors occurred while online tuning was enabled (A1-02 = 2):
Remedy: Set E2-02, E2-03, and E2-06 to the correct values. |
| oPE27 Flow Meter Input | Cause:
Remedy:
|
| oPE30 Incorrect Input Voltage Adjustment | Cause: The input voltage offset adjustment has not been performed.
Remedy: Contact Yaskawa or your nearest sales representative for information on clearing the error. |
| oPE31 Water Level/Suction Pressure/PI Aux Cause | Cause: One or both of the following conditions are present:
Remedy: Confirm parameter settings of Q4-01, Q5-01, Q6-01, H3-02, H3-06 and H3-10. |
| oPE34 De-Scale Setting Error | Cause: The De-scale function is not allowed while Anti-Jam is enabled. Remedy: Review settings of parameters P1-01, P7-01, or P8-01. |
| End1 Excessive V/f Setting (detected only during Rotational Auto-Tuning) | Cause: The torque reference exceeded 20% during Auto-Tuning OR The results from Auto-Tuning the no-load current exceeded 80%. Remedy:
|
| End2 Motor Iron-Core Saturation Coefficient | Cause: Motor data entered during Auto-Tuning was incorrect. Remedy:
Cause: Results from Auto-Tuning are outside the parameter setting range, assigning the iron-core saturation coefficients (E2-07 and E2-08) to temporary values. Remedy:
|
| End3 Rated Current Setting Alarm | Cause: The correct current rating printed on the motor nameplate was not entered into T1-04. Remedy:
|
| End4 Adjusted Slip Calculation Error | Cause: The calculated slip is outside the allowable range. Remedy:
|
| End5 Resistance Tuning Error | Cause: The calculated resistance value is outside the allowable range. Remedy:
|
| End6 Leakage Inductance Alarm | Cause: The calculated leakage inductance value is outside the allowable range. Remedy:
|
| End7 No-Load Current Alarm | Cause: The entered no-load current value was outside the allowable range. Remedy:
Cause: Auto-Tuning results were less than 5% of the motor rated current. Remedy:
|
| Er-01 Motor Data Error | Cause: Motor data or data entered during Auto-Tuning was incorrect. Remedy:
Cause: Motor output power and motor-rated current settings (T1-02 and T1-04) do not match. Remedy:
Cause: Motor rated current and detected no-load current are inconsistent. Remedy:
|
| Er-02 Minor Fault | Cause: An alarm was triggered during Auto-Tuning. Remedy:
|
| Er-03 STOP Button Input | Cause: Auto-Tuning canceled by pressing STOP button. Remedy:
|
| Er-04 Line-to-Line Resistance Error | Cause: Motor data entered during Auto-Tuning was incorrect. Remedy:
Cause: Results from Auto-Tuning are outside the parameter setting range or the tuning process took too long. (Faulty motor cable or cable connection). Remedy:
|
| Er-05 No-Load Current Error | Cause: Motor data entered during Auto-Tuning was incorrect. Remedy:
Cause: Results from Auto-Tuning are outside the parameter setting range or the tuning process took too long. Remedy:
Cause: The load was too high during Rotational Auto-tuning. Remedy:
|
| Er-08 Rated Slip Error | Cause: Motor data entered during Auto-Tuning was incorrect. Remedy:
Cause: Results from Auto-Tuning are outside the parameter setting range or the tuning process took too long. Remedy:
Cause: The load was too high during rotational Auto-tuning. Remedy:
|
| Er-09 Acceleration Error | Cause: The motor did not accelerate for the specified acceleration time. Remedy:
Cause: Torque limit when motoring is too low (L7-01 and L7-02). Remedy:
Cause: The load was too high during Rotational Auto-Tuning. Remedy:
|
| Er-11 Motor Speed Fault | Cause: Torque reference is too high. Remedy:
|
| Er-12 Current Detection Error | Cause: One of the motor phases is missing (U/T1, V/T2, W/T3). Remedy:
Cause: The current exceeded the current rating of the drive. Remedy:
Cause: The current is too low. (Attempted Auto-Tuning without motor connected to the drive). Remedy:
Cause: Current detection signal error. Remedy:
|
| Er-13 Leakage Inductance Error | Cause: Drive was unable to complete tuning for leakage inductance within 300 seconds. Remedy:
|
| Er-17 Reverse Prohibited Error | Cause: Drive is prohibited from rotating the motor in reverse while attempting to perform Inertia Tuning. Remedy:
|
| CoPy Writing Parameter Settings (flashing) | Cause: Parameters are being written to the drive. Remedy: This is not an error. |
| CPyE Error Writing Data | Cause: Failed writing parameters. Remedy: Attempt to write parameters again. |
| CSEr Copy Unit Error | Cause: Hardware fault. Remedy: Replace the HOA keypad or the USB Copy Unit. |
| dFPS Drive Model Mismatch | Cause: The drives used in the copy and write process are not the same model.
Remedy:
|
| End Task Complete | Cause: Finished reading, writing, or verifying parameters. Remedy: This is not an error. |
| iFEr Communication Error | Cause:
Remedy:
|
| ndAT Model, Voltage Class, Capacity Mismatch | Cause:
Remedy:
|
| rdEr Error Reading Data | Cause: Failed while attempting to read parameter settings from the drive. Remedy: Press and hold the READ key on the USB Copy Unit for at least one second to have the unit read parameters from the drive. |
| rEAd Reading Parameter Settings (flashing) | Cause: Displayed while the parameter settings are being read onto the USB Copy Unit. Remedy: This is not an error. |
| vAEr Voltage Class, Capacity Mismatch | Cause: The drive from which the parameters were copied and the drive on which the Verify mode is being performed have different electrical specifications or are a different capacity. Remedy: Make sure electrical specifications and capacities are the same for both drives. |
| vFyE Parameter settings in the drive and those saved to the copy function are not the same | Cause: Indicates that parameter settings that have been Read and loaded onto the Copy Unit or HOA keypad are different. Remedy: To synchronize parameters, either write the parameters saved on the USB Copy Unit or HOA keypad onto the drive, or Read the parameter settings on the drive onto the USB Copy Unit. |
| vrFy Comparing Parameter Settings (flashing) | Cause: The Verify mode has confirmed that parameters settings on the drive and parameters read to the copy device are identical. Remedy: This is not an error. |
Anti Jam Active Anti-Jam Function Status | Cause: Displayed when the drive is performing the anti-jam function. Remedy: Information only. No action required. |
De-staging in X sec De-staging Timer Status | Cause: Displayed during multiplexing when either a drive or contactor de-staging is in progress. X sec indicates the time left before the de-staging takes place. Remedy: Information only. Wait for timer to expire. |
DigitalOut Delay Active Output Delay Status | Cause: Displayed when the Digital Output Delay function is active. Remedy: Information only. |
Feedback Drop Check Sleep Mode Feedback Check | Cause: Displayed when the drive is determining whether the feedback will change abruptly when the drive enters Sleep Mode. Remedy: Check configuration: Drop Level is configured by P2-08, Delta Sleep Feedback Drop Level, and P2-09 Feedback Detection Drop Time. |
Flow Rate Limit Speed Limited by Flow Rate | Cause: Drive output speed is being limited due to the Flow Rate (U1-83). Remedy: Check Flow Rate settings if limitation is unexpected. |
Freq Reduction Active (P3-07) Staging Frequency Reduction | Cause: Maximum Frequency temporarily reduced due to Staging. Remedy: Information only. |
LOCK Parameter Locked Write Protection Active | Cause: Displayed after an attempt to change a parameter when A1-01 = 3. Remedy: Unlock the keypad by setting A1-01 = 2. |
Lube Pump Exit in Xsec Lube Pump Delay | Cause: The drive is delaying the start of the motor and the Lube Pump (H2-xx = 8B) digital output is energized. Remedy: Wait for timer (Xsec) to expire. |
PASS MEMOBUS/Modbus Comm. Test Mode Complete Test Result | Cause: MEMOBUS/Modbus test has finished normally. Remedy: Information only. |
Pre Chg Mode Exit in Xsec Pre-Charge Active | Cause: Pre-Charge 1 or 2 active. X indicates time left before pre-charge exits due to timers (P4-03 + P4-07). Remedy: Wait for timer to expire. |
Primer Pump Exit in Xsec Primer Pump Delay | Cause: The drive is delaying the start of the motor and the Primer Pump (H2-xx = 8B) digital output is energized. Remedy: Wait for timer to expire. |
ScreenMtrStarter Exit in Xsec Screen Motor Starter Delay | Cause: The drive is delaying the start of the motor and the Screen Motor Starter (H2-xx = 8B) digital output is energized. Remedy: Wait for timer to expire. |
Setpoint Boost Active (P3-11) Staging Frequency Reduction | Cause: Maximum Frequency temporarily reduced due to Staging. Remedy: Information only. |
Sleep Active Min/Max PIAuxLvl Sleep Mode (Aux Level) | Cause: Displayed when the PI Aux Feedback falls below the Q6-04/Q6-24 level for longer than the Q6-05 time forcing the drive to go to a sleep condition. Remedy: Check Q6-04/Q6-24 levels and Q6-05 timer if sleep is unexpected. |
Sleep Active Min Suction Pres Sleep Mode (Suction Pressure) | Cause: Displayed when the drive has gone to sleep because the suction level has dropped below the level set in Q5-04 for longer than the time set in Q5-05. Remedy: Check suction levels; verify settings Q5-04 and Q5-05. |
Sleep Active Min Water Level Sleep Mode (Water Level) | Cause: Displayed when the drive has gone to sleep because the water level has dropped below the level set in Q4-04 for longer than the time set in Q4-05. Remedy: Check water levels; verify settings Q4-04 and Q4-05. |
Sleep Active Wait for Start Sleep Mode Standby | Cause: Displayed when the drive is in Sleep Mode or when the drive is waiting for the feedback level to reach the level set in P1-04, Start Level. Remedy: Wait for feedback to reach P1-04 level. |
Sleep AUTO -> Off AUTO Cmd to RUN Sleep Enabled Status | Cause: Displayed when parameter P2-15 is set to 1 (Enabled) and drive has turned-off due to Sleep. Remedy: Information only. |
Sleep Boost Active Sleep Mode Pressure Boost | Cause: Displayed when the drive entering Sleep Mode and the pressure setpoint is being boosted. During this time, the U1-01, Frequency Reference, monitor will be updated with the boosted setpoint. Remedy: Information only. |
Staging in X sec Staging Timer Status | Cause: Displayed during multiplexing when either a drive or contactor staging is in progress. X sec indicates the time left before the staging takes place. Remedy: Information only. Wait for timer to expire. |
Start Delay Adjust b1-11 Back Spin Timer Active | Cause: Displayed when the drive start is being delayed by Coast to Stop with Timer (Back Spin Timer). Remedy: This time is adjusted by parameter b1-11, Coast to Stop with Timer Time. |
Start Delay Timer Active Start Delay Active | Cause: Displayed when the feedback level has reached the level set in P1-04, Start Level, and the Start Delay timer is incrementing. Remedy: Information only. |
Thrust Mode Thrust Active Thrust Mode Status | Cause: Displayed during Thrust Mode. Remedy: Information only. |
Utility Delay Adjust by P4-17 Utility Start Delay Status | Cause: Displayed when the drive is delaying the Run command due to the Utility Start Delay Function. Remedy: Information only. Delay controlled by P4-17. |