ABB ACS355 Drive

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Below image show terminal details:

Model no.R. MinR. MaxP.BR Max
1-phase, 200 to 240 VohmohmKW
ACS355-01x-02A4-2703900.37
ACS355-01x-04A7-2402000.75
ACS355-01x-06A7-2401301.1
ACS355-01x-07A5-2301001.5
ACS355-01x-09A8-230702.2
3-phase, 380 to 480 V
ACS355-03x-01A2-420011800.37
ACS355-03x-01A9-41758000.55
ACS355-03x-02A4-41655900.75
ACS355-03x-03A3-41504001.1
ACS355-03x-04A1-41303001.5
ACS355–03x-05A6-41002002.2
ACS355-03x-07A3-4701503
ACS355-03x-08A8-4701104
ACS355-03x-12A5-440805.5
ACS355-03x-15A6-440607.5
ACS355-03x-23A1-4304011
ACS355-03x-31A0-4162915
ACS355-03x-38A0-4132318.5
ACS355-03x-44A0-4131922

Search from below list for ACS355 drive faults & alarms:

CodeCause & Solution
A2001
OVERCURRENT

Cause: Output current limit controller is active.

Solution:

1. Check motor load.
2. Check acceleration time (parameters 2202 ACCELER TIME 1 and 2205 ACCELER TIME 2).
3. Check motor and motor cable (including phasing).
4. Check ambient conditions.
A2002
OVERVOLTAGE
Cause: DC overvoltage controller is active.

Solution:

1. Check deceleration time (parameters 2203 DECELER TIME 1 and 2206 DECELER TIME 2).
2. Check input power line for static or transient overvoltage.
A2003
UNDERVOLTAGE
Cause: DC undervoltage controller is active.

Solution: Check input power supply.
A2004
DIRLOCK
Cause: Change of direction is not allowed.

Solution: Check parameter 1003 DIRECTION settings.
A2005
IO COMM
Cause: Fieldbus communication break.

Solution:

1. Check status of fieldbus communication.
2. Check fault function parameter settings.
3. Check connections.
4. Check if master can communicate.
A2006
AI1 LOSS
Cause: Analog input AI1 signal has fallen below limit defined by parameter 3021 AI1 FAULT LIMIT.

Solution:

1. Check fault function parameter settings.
2. Check for proper analog control signal levels.
3. Check connections.
A2007
AI2 LOSS
Cause: Analog input AI2 signal has fallen below limit defined by parameter 3022 AI1 FAULT LIMIT.

Solution:

1. Check fault function parameter settings.
2. Check for proper analog control signal levels.
3. Check connections.
A2008
PANEL LOSS
Cause: Control panel selected as active control location for drive has ceased communicating.

Solution:

1. Check panel connection.
2. Check fault function parameters.
3. Check control panel connector.
4. Refit control panel in mounting platform.
5. If drive is in external control mode (REM) and is set to accept start/stop, direction commands or references through control panel:
Check group 10 START/STOP/DIR and 11 REFERENCE SELECT settings.
A2009
DEVICE OVERTEMP
Cause: Drive IGBT temperature is excessive. Alarm limit is 120 °C.

Solution:

1. Check ambient conditions.
2. Check air flow and fan operation.
3. Check motor power against drive power.
A2010
MOTOR TEMP
Cause: Motor temperature is too high (or appears to be too high) due to excessive load, insufficient motor power, inadequate cooling or incorrect start-up data.

Solution:

1. Check motor ratings, load and cooling.
2. Check start-up data.
3. Check fault function parameter settings.
4. Let motor cool down.
5. Ensure proper motor cooling: Check cooling fan, clean cooling surfaces, etc.
A2011
UNDERLOAD
Cause: Motor load is too low due to, for example, release mechanism in driven equipment.

Solution:

1. Check for problem in driven equipment.
2. Check fault function parameter settings.
3. Check motor power against drive power.
A2012
MOTOR STALL
Cause: Motor is operating in stall region due to, for example, excessive load or insufficient motor power.

Solution:

1. Check motor load and drive ratings.
2. Check fault function parameter settings.
A2013
AUTORESET
Cause: Automatic reset alarm.

Solution: Check parameter group 31 AUTOMATIC RESET settings.
A2018
PID SLEEP
Cause: Sleep function has entered the sleeping mode.

Solution: See parameter groups 40 PROCESS PID SET 1… 41 PROCESS PID SET 2.
A2019
ID RUN
Cause: Motor Identification run is on.

Solution: This alarm belongs to normal start-up procedure. Wait until drive indicates that motor identification is completed.
A2021
START ENABLE 1
MISSING
Cause: No Start enable 1 signal received.

Solution:

1. Check parameter 1608 START ENABLE 1 settings.
2. Check digital input connections.
3. Check fieldbus communication settings.
A2022
START ENABLE 2
MISSING
Cause: No Start enable 2 signal received.

Solution:

1. Check parameter 1609 START ENABLE 2 settings.
2. Check digital input connections.
3. Check fieldbus communication settings.
A2023
EMERGENCY
STOP
Cause: Drive has received emergency stop command and ramps to stop according to ramp time defined by parameter 2208 EMERG DEC TIME.

Solution:

1. Check that it is safe to continue operation.
2. Return emergency stop push button to normal position.
A2024
ENCODER
ERROR
Cause: Communication fault between pulse encoder and pulse encoder interface module or between module and drive.

Solution:

1. Check pulse encoder and its wiring, pulse encoder interface module and its wiring and parameter group 50 ENCODER settings.
2. This is a programmable fault function, check parameter 5003.
A2025
FIRST START
Cause: Motor identification magnetization is on. This alarm belongs to normal start-up procedure.

Solution: Wait until drive indicates that motor identification is completed.
A2026
INPUT
PHASE
LOSS
Cause: Intermediate circuit DC voltage is oscillating due to missing input power line phase or blown fuse. Alarm is generated when DC voltage ripple exceeds 14% of nominal DC voltage.

Solution:

1. Check input power line fuses.
2. Check for input power supply imbalance.
3. Check fault function parameter setting.
4. This is a programmable fault function, check parameter 3016 SUPPLY PHASE
A2029
MOTOR BACK
EMF
Cause: Permanent magnet synchronous motor is rotating, start mode 2 (DC MAGN) is selected with parameter 2101 START FUNCTION, and run is requested. Drive warns that rotating motor cannot be magnetized with DC current.

Solution: If start to rotating motor is required, select start mode 1 (AUTO) with parameter 2101 START FUNCTION. Otherwise drive starts after motor has stopped.
A2035
SAFE TORQUE
OFF
Cause: STO (Safe torque off) requested and it functions correctly. Parameter 3025 STO OPERATION is set to react with alarm.

Solution:

1. If this was not expected reaction to safety circuit interruption, check cabling of safety circuit connected to STO terminals X1C.
2. If different reaction is required, change value of parameter 3025 STO OPERATION.

Note: Start signal must be reset (toggled to 0) if STO has been used while drive has been running.
A5001 Cause: Drive is not responding.

Solution: Check panel connection.
A5002 Cause: Incompatible communication profile.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5010 Cause: Corrupted panel parameter backup file

Solution:

1. Retry parameter upload.
2. Retry parameter download.
A5011 Cause: Drive is controlled from another source.
Solution: Change drive control to the local control mode.
A5012 Cause: Direction of rotation is locked.

Solution: Enable change of direction. See parameter 1003 DIRECTION.
A5013 Cause: Panel control is disabled because start inhibit is active.

Solution:

1. Start from the panel is not possible. Reset the emergency stop command or remove the 3-wire stop command before starting from the panel.
2. Check parameters 1001 EXT1 COMMANDS, 1002 EXT2 COMMANDS and 2109 EMERG STOP SEL.
A5014Cause: Panel control is disabled because of drive fault.

Solution: Reset drive fault and retry.
A5015 Cause: Panel control is disabled because the local control mode lock is active.

Solution: Deactivate the local control mode lock and retry. See parameter 1606 LOCAL LOCK.
A5018 Cause: Parameter default value is not found.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5019Cause: Writing non-zero parameter value is prohibited.

Solution: Only parameter reset is allowed.
A5020 Cause: Parameter or parameter group does not exist or parameter value is inconsistent.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5021 Cause: Parameter or parameter group is hidden.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5022 Cause: Parameter is write protected.

Solution: Parameter value is read-only and cannot be changed.
A5023Cause: Parameter change is not allowed, when drive is running.

Solution: Stop drive and change parameter value.
A5024 Cause: Drive is executing task.

Solution: Wait until task is completed.
A5025 Cause: Software is being uploaded or downloaded.

Solution: Wait until upload/download is complete.
A5026Cause: Value is at or below minimum limit.
A5027Cause: Value is at or above maximum limit.
A5028Cause: Invalid value
A5029 Cause: Memory is not ready.

Solution: Retry.
A5030 Cause: Invalid request
A5031 Cause: Drive is not ready for operation, for example, due to low DC voltage.

Solution: Check input power supply.
A5032Cause: Parameter error.
A5040 Cause: Parameter download error. Selected parameter set is not in current parameter backup file.

Solution: Perform upload function before download.
A5041 Cause: Parameter backup file does not fit into memory.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5042 Cause: Parameter download error. Selected parameter set is not in current parameter backup file.

Solution: Perform upload function before download.
A5043Cause: No start inhibit.
A5044 Cause: Parameter backup file restoring error.

Solution:

1. Check that file is compatible with drive.
A5050 Cause: Parameter upload aborted.

Solution:

1. Retry parameter upload.
A5051Cause: File error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5052Cause: Parameter upload has failed.

Solution: Retry parameter upload.
A5060 Cause: Parameter download aborted.

Solution:

1. Retry parameter download.
A5062Cause: Parameter download has failed.

Solution: Retry parameter download.
A5070 Cause: Panel backup memory write error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5071 Cause: Panel backup memory read error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.

A5080
Cause: Operation is not allowed because the drive is not in the local control mode.

Solution: Switch to the local control mode.
A5081 Cause: Operation is not allowed because of active fault.

Solution: Check cause of fault and reset fault.
A5083Cause: Operation is not allowed because parameter lock is on.


Solution: Check parameter 1602 PARAMETER LOCK setting.
A5084 Cause: Operation is not allowed because drive is performing a task.

Solution: Wait until task is completed and retry.
A5085Cause: Parameter download from source to destination drive has failed.

Solution:

1. Check that source and destination drive types are same, ie ACS310. See the type designation label of the drive.
A5086Cause: Parameter download from source to destination drive has failed.

Solution:

1. Check that source and destination drive type designations are the same.
2. See type designation labels of the drives.
A5087 Cause: Parameter download from source to destination drive has failed because parameter sets are incompatible.

Solution:

1. Check that source and destination drive information are same. See parameters in group 33 INFORMATION.
A5088 Cause: Operation has failed because of drive memory error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5089 Cause: Download has failed because of CRC error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5090 Cause: Download has failed because of data processing error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5091Cause: Operation has failed because of parameter error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
A5092Cause: Parameter download from source to destination drive has failed because parameter sets are incompatible.

Solution:

1. Check that source and destination drive information are same. See parameters in group 33 INFORMATION.
F0001
OVERCURRENT
Cause: Output current has exceeded trip level. Overcurrent trip limit for drive is 325% of drive nominal current.

Solution:

1. Check motor load.
2. Check acceleration time (parameters 2202 ACCELER TIME 1 and 2205 ACCELER TIME 2).
3. Check motor and motor cable (including phasing).
4. Check ambient conditions. Load capacity decreases if installation site ambient temperature exceed 40 °C.
F0002
DC OVERVOLT
Cause: Excessive intermediate circuit DC voltage. DC overvoltage trip limit is 420 V for 200 V drives and 840 V for 400 V drives.

Solutions:
1. Check that overvoltage controller is on (parameter 2005 OVERVOLT CTRL).
2. Check brake chopper and resistor (if used). DC overvoltage control must be deactivated when brake chopper and resistor are used.
3. Check deceleration time (parameters 2203 DECELER TIME 1 and 2206 DECELER TIME 2).
4. Check input power line for static or transient overvoltage.
5. Retrofit frequency converter with brake chopper and brake resistor.
F0003
DEV OVERTEMP
Cause: Drive IGBT temperature is excessive. Fault trip limit is 135 °C.

Solution:

1. Check ambient conditions.
2. Check air flow and fan operation.
3. Check motor power against drive power.
F0004
SHORT CIRC
Cause: Short circuit in motor cable(s) or motor

Solution:

1. Check motor and motor cable.
F0006
DC UNDERVOLTAGE
Cause: Intermediate circuit DC voltage is not sufficient due to missing input power line phase, blown fuse, rectifier bridge internal fault or too low input power.

Solution:

1. Check that undervoltage controller is on (parameter 2006 UNDERVOLT CTRL).
2. Check input power supply and fuses.
F0007
AI1 LOSS
Cause: Analog input AI1 signal has fallen below limit defined by parameter 3021 AI1 FAULT LIMIT.

Solution:

1. Check fault function parameter settings.
2. Check for proper analog control signal levels.
3. Check connections.
F0008
AI1 LOSS
Cause: Analog input AI2 signal has fallen below limit defined by parameter 3022 AI2 FAULT LIMIT.

Solution:

1. Check fault function parameter settings.
2. Check for proper analog control signal levels.
3. Check connections.
F0009
MOT OVERTEMP
Cause: Motor temperature is too high (or appears to be too high) due to excessive load, insufficient motor power, inadequate cooling or incorrect start-up data.

Solution:

1. Check motor ratings, load and cooling.
2. Check start-up data.
3. Check fault function parameter settings.
4. Let motor cool down. Ensure proper motor cooling:
5. Check cooling fan, clean cooling surfaces, etc.
F0010
PANEL LOSS
Cause: Control panel selected as active control location for drive has ceased communicating.

Solution:

1. Check panel connection.
2. Check fault function parameters.
3. Check control panel connector.
4. Refit control panel in mounting platform.
5. If drive is in external control mode (REM) and is set to accept start/stop, direction commands or references through control panel:
Check group 10 START/STOP/DIR and 11 REFERENCE SELECT settings.
F0011
ID RUN
FAIL
Cause: Motor ID run is not completed successfully.

Solution:

1. Check motor connection.
2. Check start-up data (group 99 START- UP DATA).
3. Check maximum speed (parameter 2002). It should be at least 80% of motor nominal speed (parameter 9908).
4. Ensure ID run has been performed
F0012
MOTOR STALL
Cause: Motor is operating in stall region due to, for example, excessive load or insufficient motor power.

Solution:

1. Check motor load and drive ratings.
2. Check fault function parameter settings.
F0014
EXT FAULT 1
Cause: External fault 1 Check external devices for faults.

Solution:

1. Check fault function parameter setting.
F0015
EXT FAULT 2
Cause: External fault 2

Solution:

1. Check external devices for faults.
2. Check fault function parameter setting.
F0016
EARTH FAULT
Cause: Drive has detected earth (ground) fault in motor or motor cable.

Solution:

1. Check motor.
2. Check motor cable.
3. Motor cable length must not exceed maximum specifications.

Note: Disabling earth fault (ground fault) may
damage drive.
F0017
UNDERLOAD
Cause: Motor load is too low due to, for example, release mechanism in driven equipment.

Solution:

1. Check for problem in driven equipment.
2. Check fault function parameter settings.
3. Check motor power against drive power.
F0018
THERM FAIL
Cause: Drive internal fault. Thermistor used for drive internal temperature measurement is open or short-circuited.

Solution: This hardware issue in drive need to repair or replace drive.
F0021
CURRENT MEAS
Cause: Drive internal fault. Current measurement is out of range.

Solution: This hardware issue in drive need to repair or replace drive.
F0022
Supply PHASE
LOSS
Cause: Intermediate circuit DC voltage is oscillating due to missing input power line phase or blown fuse. Fault trip occurs when DC voltage ripple exceeds 14% of nominal DC voltage.

Solution:

1. Check input power line fuses.
2. Check for input power supply imbalance.
3. Check fault function parameter setting.
F0023
ENCODER
ERROR
Cause: Communication fault between pulse encoder and pulse encoder interface module or between module and drive.

Solution:

1. Check pulse encoder and its wiring, pulse encoder interface module and its wiring and parameter group 50 ENCODER settings.
F0024
OVERSPEED
Cause: Motor is turning faster than highest allowed speed due to incorrectly set minimum/maximum speed.
Operating range limits are set by parameters 2007 MINIMUM FREQ and 2008 MAXIMUM FREQ.

Solution:

1. Check minimum/maximum frequency settings.
2. Check adequacy of motor braking torque.
F0027
CONFIG FILE
Cause: Internal configuration file error.

Solution: This hardware issue in drive need to repair or replace drive.
F0028
SERIAL 1 ERR
Cause: Fieldbus communication break.

Solution:

1. Check status of fieldbus communication.
2. Check fault function parameter settings.
3. Check connections.
4. Check if master can communicate.
F0029
EFB CON FILE
Cause: Configuration file reading error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0030
FORCE TRIP
Cause: Trip command received from fieldbus

Solution: See appropriate communication module manual.
F0034
MOTOR PHASE
Cause: Motor circuit fault due to missing motor phase or motor thermistor relay (used in motor temperature measurement) fault.

Solution:

1. Check motor and motor cable.
2. Check motor thermistor relay (if used).
F0035
OUTPUT WIRING
Cause: Incorrect input power and motor cable connection (that is input power cable is connected to drive motor connection).
Fault can be erroneously declared if drive is faulty or input power is delta grounded system and motor cable capacitance is large.

Solution:

1. Check input power connections.
2. Check input & output connection.
F0036
INCOMPATIBLE
SW
Cause: Loaded software is not compatible.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0037
CB OVERTEMP
Cause: Drive control board overheated. Fault given when measured temperature of the control board (indicated by signal 0150 CB TEMP) reaches 95 °C for an IP20 drive or 102 °C for an IP66 drive (ACS355-…+B063).

Parameter 3024 CB TEMP FAULT is set to enable with fault.

Solution:

1. Check for excessive ambient temperature.
2. Check for fan failure.
3. Check for obstructions in air flow.
4. Check the dimensioning and cooling of cabinet.
F0044
SAFE TORQUE
OFF
Cause: STO (Safe torque off) requested and it functions correctly.

Parameter 3025 STO OPERATION is set to react with fault.

Solution:

1. If this was not expected reaction to safety circuit interruption, check cabling of safety circuit connected to STO terminals X1C.
2. If different reaction is required, change value of parameter 3025 STO OPERATION.
3. Reset fault before starting.
F0045
STO1 LOST
Cause: STO (Safe torque off) input channel 1 has not de-energized, but channel 2 has. Opening contacts on channel 1 might have been damaged or there is a short-circuit.

Solution:

1. Check STO circuit cabling and opening of contacts in STO circuit.
F0046
STO2 LOST
Cause: STO (Safe torque off) input channel 2 has not de-energized, but channel 1 has. Opening contacts on channel 2 might have been damaged or there is a short-circuit.

Solution:

1. Check STO circuit cabling and opening of contacts in STO circuit.
F0101
SERF CORRUPT
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0103
SERF MACRO
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0201
DSP T1
OVERLOAD
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0202
DSP T2
OVERLOAD
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0203
DSP T3
OVERLOAD
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0204
DSP STACK
ERROR
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F0206
CB ID ERROR
Cause: Drive internal error.

Solution: There is an hardware or software issue in drive, need to repaur or replace drive.
F1000
PAR HZRPM
Cause: Incorrect speed/frequency limit parameter setting

Solution:

1. Check parameter settings.
2. Following must apply: 2007 MINIMUM FREQ < 2008 MAXIMUM FREQ,
3. 2007 MINIMUM FREQ/9907 MOTOR NOM FREQ and 2008 MAXIMUM FREQ/9907 MOTOR NOM FREQ are within range.
F1003
PAR AI SCALE
Cause: Incorrect analog input AI signal scaling.

Solution:

1. Check parameter group 13 ANALOG INPUTS settings.
2. Check that following applies:
• 1301 MINIMUM AI1 < 1302 MAXIMUM AI1
• 1304 MINIMUM AI2 < 1305 MAXIMUM AI2.
F1004
PAR AO SCALE
Cause: Incorrect analog output AO signal scaling.

Solution:

1. Check parameter group 15 ANALOG OUTPUTS settings.
2. Check that following applies:
• 1504 MINIMUM AO1 < 1505 MAXIMUM AO1.
F1005
PAR PCU 2
Cause: Incorrect motor nominal power setting.

Solution:

Check parameter 9909 MOTOR NOM POWER setting. Following must apply:
• 1.1 < (9906 MOTOR NOM CURR · 9905 MOTOR NOM VOLT · 1.73 / PN ) < 3.0 Where PN = 1000 · 9909 MOTOR NOM POWER (if units are in kW) or PN = 746 · 9909 MOTOR NOM POWER (if units are in hp).
F1006
PAR EXT RO
Cause: Incorrect extension relay output parameters

Solution:

1. Check parameter settings.
2. Check that following applies:
• MREL relay output extension module is connected to the drive.
• 1402…1403 RELAY OUTPUT 2 … RELAY OUTPUT 3 and 1410 RELAY OUTPUT 4 have non-zero values.
F1007
PAR FBUSMISS
Cause: Fieldbus control has not been activated.

Solution:

1. Check fieldbus parameter settings.
F1009
PAR PCU 1
Cause: Incorrect motor nominal speed/frequency setting.

Solution:

1. Check parameter settings.
2. Following must apply for induction motor:
• 1 < (60 · 9907 MOTOR NOM FREQ / 9908 MOTOR NOM SPEED) < 16
• 0.8 < 9908 MOTOR NOM SPEED / (60 · 9907 MOTOR NOM FREQ / 9913 MOTOR POLE PAIRS) < 0.992
3. Following must apply for permanent magnet synchronous motor:
• 9908 MOTOR NOM SPEED / (60 · 9907 MOTOR NOM FREQ / 9913 MOTOR POLE PAIRS) = 1.0
F1015
PAR USER
DEFINED U/F
Cause: Incorrect voltage to frequency (U/f) ratio voltage setting.

Solution:

1. Check parameter 2610 USER DEFINED U1…2617 USER DEFINED F4 settings.
F1017
PAR SETUP 1
Cause: It is not allowed to use frequency input signal and frequency output signal simultaneously.

Solution:

1. Disable frequency output or frequency input:
• change transistor output to digital mode (value of parameter 1804 TO MODE = DIGITAL), or
• change frequency input selection to other value in parameter groups
11 REFERENCE SELECT,
40 PROCESS PID SET 1,
41 PROCESS PID SET 2 and
42 EXT / TRIM PID.