Fuji FRENIC-MEGA Drive

Fault CodeCause & Solution
OCn
Overcurrent
Cause & Solution:

1. Ground fault or short circuit exists in the output circuit.
– Check whether short-circuit occurs on the motor, the motor cable or contactor.
2. Acceleration time is too short.
– Increase acceleration time.
3. Customized torque boost or V/F curve is not appropriate.
– Adjust the customized torque boost or V/F curve.
4. The voltage is too low.
– Adjust the voltage to normal range.
5. The spinning motor is started.
– Enable the catching a spinning motor function or start the motor after it stops.
6. A load is applied suddenly during acceleration.
– Cancel the suddenly added load.
7. The rated AC drive power is low.
– Replace the drive by one with higher rated power.
8. The braking resistor resistance is small.
– The braking resistor is short circuited.
– Replace a new braking resistor.
OC1
Overcurrent
during
acceleration
Cause & Solution:

1. Ground fault or short circuit exists in the output circuit.
– Check whether short-circuit occurs on the motor, the motor cable or contactor.
2. Acceleration time is too short.
– Increase acceleration time.
3. Customized torque boost or V/F curve is not appropriate.
– Adjust the customized torque boost or V/F curve.
4. The voltage is too low.
– Adjust the voltage to normal range.
5. The spinning motor is started.
– Enable the catching a spinning motor function or start the motor after it stops.
6. A load is applied suddenly during acceleration.
– Cancel the suddenly added load.
7. The rated AC drive power is low.
– Replace the drive by one with higher rated power.
8. The braking resistor resistance is small.
– The braking resistor is short circuited.
– Replace a new braking resistor.
OC2
Overcurrent
during
deceleration
Cause & Solution:

1. Ground fault or short circuit exists in the output circuit.
– Check whether short-circuit occurs on motor, motor cable or contactor.

2. Acceleration time is too short.
– Increase acceleration time.

3. The voltage is too low.
– Adjust the voltage to normal range.

4. A load is added suddenly during deceleration.
– Cancel the suddenly added load.

5. Braking unit and braking resistor are not installed.
– Install the braking unit and braking resistor.

6. The braking resistor resistance is small or the braking resistor is short circuited.
– Replace a new braking resistor.
OC3
Overcurrent
at constant
speed
Cause & Solution:

1. Ground fault or short circuit exists in the output circuit.
– Check whether short-circuit occurs on the motor, motor cable or contactor

2. The voltage is too low.
– Adjust the voltage to normal range.

3. A load is added suddenly during running.
– Cancel the suddenly added load.

4. The rated AC drive power is low.
– Replace the drive by one with higher rated power.

5. The braking resistor resistance is small or the braking resistor is short circuited.
– Replace a new braking resistor.
EF
Earth
fault
Cause: A earth fault current flew from the output terminal of the inverter.

Solution:

1. The output terminal of the inverter is short-circuited to the ground (ground fault, or earthed).
– Disconnect the wires from the output terminals ([U], [V], and [W]) and perform a megger test.
– Remove the earthed path (including the replacement of the wires, the terminals, or the motor as necessary).
OUn
Overvoltage
Cause & Solution:

1. Input voltage is too high.
– Adjust input voltage to normal range.

2. An external force drives motor during acceleration.
– Cancel the external force.

3. Braking unit and braking resistor are not installed.
– Install the braking unit and braking resistor.

4. Acceleration time is too short.
– Increase acceleration time.
OV1/OU1
Overvoltage
during
acceleration
Cause & Solution:

1. Input voltage is too high.
– Adjust input voltage to normal range.

2. An external force drives motor during acceleration.
– Cancel the external force.

3. Braking unit and braking resistor are not installed.
– Install the braking unit and braking resistor.

4. Acceleration time is too short.
– Increase acceleration time.
OV2/OU2
Overvoltage
during
deceleration
Cause & Solution:

1. Input voltage is too high.
– Adjust input voltage to normal range.

2. An external force drives motor during deceleration.
– Cancel the external force or install the braking resistor.

3. Deceleration time is too short.
– Increase deceleration time.

4. Braking unit and braking resistor are not installed.
– Install the braking unit and braking resistor.
OV3/OU3
Overvoltage
at constant
speed
Cause & Solution:

1. Input voltage is too high.
– Adjust input voltage to normal range.

2. An external force drives motor during running.
– Cancel the external force or install a braking resistor.
LU/LV
Undervoltage
Cause & Solution:

1. An instantaneous power failure occurs.
– Reset the fault

2. The AC drive’s input voltage is not within the permissible range.
– Adjust the voltage to normal range.

3. The bus voltage is abnormal.
– Replace the AC drive.

4. The rectifier bridge, the pre-charge resistor, the drive board or the control board are abnormal.
– Replace the AC drive.
Lin
Input phase
loss
Cause & Solution:

1. Three phase input is abnormal.
– Eliminate faults in external circuitry

2. Drive board is abnormal.
– Eliminate faults in external circuitry

3. Lightning protection board is abnormal.
– There is an hardware or software issue in drive. Need to repair or replace drive.


4. Control board is abnormal.
– There is an hardware or software issue in drive. Need to repair or replace drive.
OPL
Output phase
loss
Cause & Solution:

1. Motor winding is damaged. Check resistance between motor cables.
– Replace motor is winding is damaged.

2. The cable connecting the AC drive and the motor is abnormal.
– Check for wiring errors and ensure the output cable is connected properly

3. The AC drive’s three-phase outputs are unbalanced when the motor is running.
– Check whether the motor three-phase winding is normal.

4. The drive board or the IGBT is abnormal.
– Replace the AC drive.
OH1
Heat sink
overheat
Cause & Solution:

1. The ambient temperature is too high.
– Lower the ambient temperature.

2. The ventilation is clogged.
– Clean the ventilation.

3. The fan is damaged.
– Replace the cooling fan.

4. The thermally sensitive resistor of IGBT is damaged.
– Replace the AC drive.

5. The AC drive IGBT is damaged.
– Replace the AC drive.
OH2
External
alarm input
Cause: External alarm was inputted (THR).

Solution:

1. An alarm function of the external equipment was activated.
– Inspect external equipment operation.
– Remove the cause of the alarm that occurred.

2. Connection has been performed incorrectly.
– Check if the wire for the external alarm signal is correctly connected to the terminal to which the “Alarm from external equipment” has been assigned.
– Connect the wire for the alarm signal correctly.

3. Incorrect settings.
– Check if the “Alarm from external equipment” has not been assigned to an unassigned terminal.
– Correct the assignment.
OH3
Inverter
internal
overheat
Cause: The temperature inside the inverter exceeded the allowable limit.

Solution:

1. The ambient temperature exceeded the allowable limit specified for the inverter.
– Measure the ambient temperature.
– Lower the ambient temperature by improving the ventilation.
OH4
Motor
overheat
(PTC/NTC
thermistor)
Cause: Temperature of the motor has risen abnormally.

Solution:

1. The temperature around the motor exceeded the range of the motor specification.
– Measure the temperature around the motor.

2. Cooling system for the motor defective.
– Check if the cooling system of the motor is operating normally.

3. The activation level of the PTC thermistor for motor overheat protection was set inadequately.
– Check the PTC thermistor specifications and recalculate the detection voltage.

4. Settings for the PTC/NTC thermistor are improper.
– Check the setting of the thermistor mode selection.
dbh
Braking
resistor
overheated
Cause: Problem The electronic thermal protection for the braking resistor has been activated.

Solution:

1. Braking load is too heavy. Reconsider the relationship between the estimated braking load and the real one.
– Lower the real braking load.
– Review the selection of the braking resistor and increase the braking capability.

2. Specified deceleration time is too short. Recalculate the deceleration torque and time needed for the load currently applied, based on a moment of inertia for the load and the deceleration time.
– Increase the deceleration time .
– Review the selection of the braking resistor and increase the braking capability.

3. Incorrect setting of function code data. Recheck the specifications of the braking resistor.
FUS/FU5
Fuse blown
Cause: The fuse inside the inverter blew.

Solution:

1. The fuse blew because of a short-circuiting inside the inverter.
– Check whether there has been any excess surge or noise coming from outside.
– Take measures against surges and noise.
– Have the inverter repaired.
PbF
Charger
circuit fault
Cause: The magnetic contactor for short-circuiting the resistor for charging failed to work.

Solution:

Control power was not supplied to the magnetic contactor intended for short-circuiting the charging resistor.

1. Check whether, in normal connection of the main circuit (not connection via the DC link bus), the connector on the power supply printed circuit board is not inserted to NC .
– Insert the connector to FAN .

2. Check whether you have quickly turned the circuit breaker ON and OFF to confirm safety after cabling/wiring.
– Wait until the DC link bus voltage has dropped to a sufficiently low level and then reset the current alarm, and turn ON the power again. (Do not turn the circuit breaker ON and OFF quickly.)
(Turning ON the circuit breaker supplies power to the control circuit to the operation level (lighting LEDs on the keypad) in a short period. Immediately turning it OFF even retains the control circuit power for a time, while it shuts down the power to the magnetic contactor intended for short-circuiting the charging resistor since the contactor is directly powered from the main power.
– Under such conditions, the control circuit can issue a turn-on command to the magnetic contactor, but the contactor not powered can produce nothing. This state is regarded as abnormal, causing an alarm.)
OLn
Overload
of motor 1
through 3
Cause: Electronic thermal protection for motor 1, 2, or 3 activated.

Solution:

1. The electronic thermal characteristics do not match the motor overload characteristics.
– Check the motor characteristics.

2. The activation level for the electronic thermal protection was not appropriate.
– Check the continuous allowable current of the motor

3. The specified acceleration/ deceleration time was too short.
– Recalculate the acceleration/deceleration torque and time needed for the load, based on the moment of inertia for the load and the acceleration/deceleration time.

4. Overload.
– Measure the output current.
OL1
Motor 1
overload
Cause: Electronic thermal protection for motor 1 activated.

Solution:

1. The electronic thermal characteristics do not match the motor overload characteristics.
– Check the motor characteristics.

2. The activation level for the electronic thermal protection was not appropriate.
– Check the continuous allowable current of the motor

3. The specified acceleration/ deceleration time was too short.
– Recalculate the acceleration/deceleration torque and time needed for the load, based on the moment of inertia for the load and the acceleration/deceleration time.

4. Overload.
– Measure the output current.
OL2
Motor 2
overload
Cause: Electronic thermal protection for motor 2 activated.

Solution:

1. The electronic thermal characteristics do not match the motor overload characteristics.
– Check the motor characteristics.

2. The activation level for the electronic thermal protection was not appropriate.
– Check the continuous allowable current of the motor

3. The specified acceleration/ deceleration time was too short.
– Recalculate the acceleration/deceleration torque and time needed for the load, based on the moment of inertia for the load and the acceleration/deceleration time.

4. Overload.
– Measure the output current.
OL3
Motor 3
overload
Cause: Electronic thermal protection for motor 3 activated.

Solution:

1. The electronic thermal characteristics do not match the motor overload characteristics.
– Check the motor characteristics.

2. The activation level for the electronic thermal protection was not appropriate.
– Check the continuous allowable current of the motor

3. The specified acceleration/ deceleration time was too short.
– Recalculate the acceleration/deceleration torque and time needed for the load, based on the moment of inertia for the load and the acceleration/deceleration time.

4. Overload.
– Measure the output current.
OLU
Inverter
overload
Cause & Solution: Temperature inside inverter rose abnormally.

1. The load is too heavy or locked-rotor occurs on the motor.
– Reduce the load or check motor and mechanical conditions.

2. The rated AC drive power is low.
– Replace the drive by one with higher rated power.

3. Temperature around the inverter exceeded that of inverter specifications.
– Measure the temperature around the inverter.
OS/O5
Overspeed
Cause: The motor rotates in an excessive speed (Motor speed ≥ (F03 data × 1.2)

Solution:

1. Incorrect setting of function code data
– Check the motor parameter “Number of poles” (P01*).
– Specify the P01* data in accordance with the motor to be used.
– Check the maximum frequency setting (F03*).
– Specify the F03* data in accordance with the output frequency.
– Check the setting of speed limit function (d32 and d33).
– Disable the speed limit function (d32 and d33).

2. Insufficient gain of the speed controller
– Check whether the actual speed overshoots the commanded one in higher speed operation.
– Increase the speed controller gain (d03*). (Depending on the situations, reconsider the setting of the filter constant or the integral time.)

3. Noises superimposed on the PG wire.
– Check whether appropriate noise control measures have been implemented (e.g., correct grounding and routing of signal wires and main circuit wires).
– Implement noise control measures.
PG/P9
PG wire
break
Cause: The pulse generator (PG) wire has been broken somewhere in the circuit.

Solution:

1. Wire break between the pulse generator (PG) and the option.
– Check whether the PG is correctly connected to the option or any wire is broken.

2. Connection failure of speed/magnetic pole position sensor.
– Check the output wiring of the speed/magnetic pole position sensor for poor contact or the phase sequence of the AB phases and UVW phases.

3. Motor rotation direction and sensor output not matched.
– Check the motor wiring for poor contact or the phase sequence.

4. onnection failure of option card(s)
– Check whether the connector of the option card engages with that of the inverter unit.

5. PG related circuit affected by strong electrical noise.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of signal wires, communication cables, and main circuit wires).

6. Mismatch between the PG power voltage (rated) and the output voltage setting of terminal [PGP].
Er1
Memory error
Cause: Error occurred in writing the data to the memory in the inverter.

Solution:

1. While the inverter was writing data (especially initializing data), power supply was turned off and the voltage for the control circuit dropped.
– Check if pressing the PGR/RESET key resets the alarm after the function code data are initialized by setting the data of H03 to 1
– Return the initialized function code data to their previous settings, then restart the operation.

2. A high intensity noise was given to the inverter while data (especially initializing data) was being written.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of control and main circuit wires).
– Improve noise control. Alternatively, return the initialized function code data to their previous settings, then restart the operation.

3. The control circuit failed.
– Initialize the function code data by setting H03 to 1, then reset the alarm by pressing the PGR/RESET key and check that the alarm goes on.
– This problem was caused by a problem of the printed circuit board (PCB) (on which the CPU is mounted).
Er2
Keypad
communications
error
Cause: A communications error occurred between the keypad and the inverter.

Solution:

1. Break in the communications cable or poor contact.
– Check continuity of the cable, contacts and connections.
– Replace the cable.

2. A high intensity noise was given to the inverter.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of control and main circuit wires).
– Improve noise control.

3. The remote keypad malfunctioned.
– Check that alarm er2 does not occur if you connect another remote keypad to the inverter.
– Replace the remote keypad.
Er3
CPU error
Cause: A CPU error (e.g. erratic CPU operation) occurred.

Solution:

1. A high intensity noise was given to the inverter.
– Check if appropriate noise control measures have been implemented (e.g. correct grounding and routing of control and main circuit wires).
– Improve noise control.
Er4
Option card
communications
error
Cause: A communications error occurred between the option card and the inverter.

Solution:

1. There was a problem with the connection between the bus option card and the inverter.
– Check whether the connector on the bus option card is properly mating with the connector of the inverter.
– Reload the bus option card into the inverter.

2. There was a high intensity noise from outside.
– Check whether appropriate noise control measures have been implemented (e.g. correct grounding and routing of control and main circuit wires and communications cable).
– Reinforce noise control measures.
Er5
Option card
error
Cause: An error detected by the option card. Refer to the instruction manual of the option card for details.
Er6
Operation
protection
Cause: An error occurred due to incorrect operation of the motor. You incorrectly operated the inverter.

Solution:

1. The STOP key was pressed when H96 = 1 or 3. Even though a run command was present at the input terminal or the communication port, the inverter was forced to decelerate to stop and er6 was displayed.
– If this was not intended, check the setting of H96.

2. The start check function was activated when H96 = 2 or 3. When one of the following conditions occurred while a run command was present at the input, the inverter did not run and er6 was displayed:
– The power was switched on
– An alarm was released
– The inverter was switched to link command LE operation.

Review the running sequence to avoid input of the run command when er6 has occurred. If this was not intended, check the setting of H96. (To reset the alarm, turn the run command off.)
Er7
Tuning error
Cause: Auto-tuning failed.

Solution:

1. A phase was missing (There was a phase loss) in the connection between the inverter and the motor.
– Properly connect the motor to the inverter.
2. V/f or the rated current of the motor was not properly set.
3. The connection between the inverter and the motor was too long.
– Check whether the connection length between the inverter and the motor is not exceeding 50m.
– Review, and if necessary, change the layout of the inverter and the motor to shorten the connection wire.
4. The rated capacity of the motor was significantly different from that of the inverter.
– Check whether the rated capacity of the motor is smaller than that of the inverter by three or more orders of class or larger by two or more orders of class.
– Check whether it is possible to replace the inverter with one with an appropriate capacity.
5. The motor was a special type such as a high-speed motor.
Er8
RS-485
communications
error
Cause: A communications error occurred during RS-485 communications.

Solution:

1. Host controllers (e.g., PLCs and personal computers) did not operate due to incorrect settings and/or defective software/hardware.
– Check the controllers.
– Remove the cause of the controller error.

2. RS-485 converter did not operate due to incorrect connections and settings, or hardware defective.
– Check the RS-485 converter (e.g., check for poor contact).
– Change the various RS-485 converter settings, reconnect the wires, or replace the converter with a recommended device as appropriate.

3. Broken communications cable or poor contact.
– Check continuity of the cable, contacts and connections.
– Replace the cable.

4. Even though no response error detection time has been set, communications did not occur cyclically.
– Check the host controllers.
– Change the settings of host controller software, or make the no response error detection time invalid.

5. A high intensity noise was given to the inverter.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of control and main circuit wires).
– Improve noise control.
– Improve noise reduction measures on the host side.
– Replace the relay converter with a recommended insulated converter.
ErP
RS-485
communications
error
Cause: A communications error occurred during RS-485 communications.

Solution:

1. Host controllers (e.g., PLCs and personal computers) did not operate due to incorrect settings and/or defective software/hardware.
– Check the controllers.
– Remove the cause of the controller error.

2. RS-485 converter did not operate due to incorrect connections and settings, or hardware defective.
– Check the RS-485 converter (e.g., check for poor contact).
– Change the various RS-485 converter settings, reconnect the wires, or replace the converter with a recommended device as appropriate.

3. Broken communications cable or poor contact.
– Check continuity of the cable, contacts and connections.
– Replace the cable.

4. Even though no response error detection time has been set, communications did not occur cyclically.
– Check the host controllers.
– Change the settings of host controller software, or make the no response error detection time invalid.

5. A high intensity noise was given to the inverter.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of control and main circuit wires).
– Improve noise control.
– Improve noise reduction measures on the host side.
– Replace the relay converter with a recommended insulated converter.
ErF
Data save
error during
undervoltage
Cause: The inverter was unable to save data such as the frequency commands, timer operation time, and PID process command set through the keypad when the power was switched off.

Solution:

1. The control circuit voltage dropped suddenly while data was being saved when the power was turned off, because the DC link bus was rapidly discharged.
– Check how long it takes for the DC link bus voltage to drop to the preset voltage when power is turned off.
– Remove whatever is causing the rapid discharge of the DC link circuit. After pressing the PGR/RESET key and releasing the alarm, set, using a remote keypad, the data of the relevant function codes (such as the frequency commands, timer operation time, and PID process command) back to the original values and then restart the operation.

2. A high intensity noise affected the operation of the inverter while data was being saved when the power was turned off.
– Check if appropriate noise control measures have been implemented (e.g., correct grounding and routing of control and main circuit wires).
– Improve noise control. After pressing the PGR/RESET key and releasing the alarm, set, using a remote keypad, the data of the relevant function codes (such as the frequency commands, timer operation time, and PID process command) back to the original values and then restart the operation.

3. The control circuit failed. Check if erf occurs each time power is switched off.
– This problem was caused by a problem of the printed circuit board (PCB) (on which the CPU is mounted).
ErH
Hardware
error
Cause: An error occurred in the LSI on the power printed circuit board (power PCB).

Solution:

1. The capacity is not set properly on the control printed circuit board.
– The inverter capacity needs to be modified again.

2. The contents of the memory on the power supply printed circuit board are corrupted.
– The power supply printed circuit board needs to be replaced.

3. Connection problem between the control printed circuit board and the power supply printed circuit board
– Either the control printed circuit board or the power supply printed circuit board needs to be replaced.
ErE
Speed mismatch
or excessive
speed deviation
Cause: An excessive deviation appears between the speed command and the detected speed.

Solution:

1. Incorrect setting of function code data
– Check the following function code data; P01* (Motor (No. of poles)), d15 (Feedback encoder pulse count/rev), and d16 and d17 (Feedback pulse correction factor 1 and 2).
– Specify data of function codes P01*, d15, d16, and d17 in accordance with the motor and PG.

2. Overload Measure the output current.
– Reduce the load.
– Check whether any mechanical brake is activated.
– Release the mechanical brake, if any.

3. The motor speed does not increase due to the current limiter operation.
– Check the data of function code F44 (Current limiter (Level)).
– Correct the F44 data. Or, if the current limiter operation is not needed, set F43 to “0” (disabled).
– Check the data of function codes F04*, F05*, and P01* through P12* to ensure that the V/f pattern setting is right.
– Match the V/f pattern setting with the motor ratings.
– Change the function code data in accordance with the motor parameters.

4. Function code settings do not match the motor characteristics.
– Check whether the data of P01*, P02*, P03*, P06*, P07*, P08*, P09*, P10* and P12* match the parameters of the motor.
– Perform auto-tuning of the inverter, using the function code P04*.

5. Wrong wiring between the pulse generator (PG) and the inverter
– Check the wiring.
– Correct the wiring.

6. Wiring to the motor is incorrect. Check the wiring to the motor.
– Connect the inverter output terminals U, V, and W to the motor input terminals U, V, and W, respectively.

7. The motor speed does not increase due to the torque limiter operation.
– Check the data of F40 (Torque limiter 1-1).
– Change the F40 data correctly. Or, set the F40 data to “999” (Disable) if the torque limiter operation is not needed.
nrb
NTC wire
break error
Cause: A wire break is found in the NTC thermistor detection circuit.

Solution:

1. The NTC thermistor cable is broken. Check whether the motor cable is broken.
– Replace the motor cable.

2. The temperature around the motor is extremely low (lower than -30°C).
– Measure the temperature around the motor.
– Reconsider the use environment of the motor.

3. The NTC thermistor is broken. Measure the resistance of the NTC thermistor.
– Replace the motor.
Err
Simulated
failure
Cause: The LED displays the alarm err.

Solution:

1. Keep key STOP + FUNC/Data key pressed for five seconds or longer.
– To escape from this alarm state, press the PGR/RES key.
CoF
PID
feedback
wire break
Cause: The signal line of PID feedback is broken.

Solution:

1. The PID feedback signal wire is broken.
– Check whether the PID feedback signal wires are connected correctly.
– Check whether the PID feedback signal wires are connected correctly. Or, tighten the related terminal screws.
– Check whether any contact part bites the wire sheath.

2. The inverter was affected by strong electrical noise.
– Check whether appropriate noise control measures have been implemented (e.g. correct grounding and routing of signal wires, communications cables, and main circuit wires).
– Implement noise control measures.
– Separate the signal wires from the main power wires as far as possible.
dba
Braking
transistor
error
Cause: A braking transistor error is detected.
– The braking transistor is broken.

Solution:

– Check whether resistance of the braking resistor is correct or there is a misconnection of the resistor.
Rro
Positioning
control error
Cause: An excessive positioning deviation has occurred when the servo-lock function was activated.

Solution:

1. Insufficient gain in positioning control system
– Readjust the settings of J97 (Servo-lock (Gain)) and d03 (Speed control 1 P (Gain)).

2. Incorrect control completion width.
– Check whether the setting of J99 (Servo-lock (Completion width)) is correct.
– Correct the setting of J99.

3. Excessive positioning deviation.
– Check whether the setting of d78 (excessive deviation detection width) is correct.