E001
Overcurrent error |
Cause:
- A steep load change occurred or motor hunting.
- Insufficient acceleration or deceleration time.
- Output line short-circuit, ground fault, or motor lock.
- System environment changes or aging deterioration.
Remedy:
- Adjust Overcurrent suppression [bA120] or Overload limit [bA122].
- Increase acceleration time [FA-10] or deceleration time [FA-12].
- Check wiring and motor insulation.
- Clean fans/ducts or reduce motor load.
|
E005
Motor overload error |
Cause:
- Operation under heavy load continued.
- Thermal level setting [bC110] is incorrect.
- Insufficient acceleration torque or load inertia is large.
- Overvoltage suppression function is active causing current increase.
Remedy:
- Re-examine operation/load conditions.
- Adjust motor thermal level setting [bC110].
- Increase acceleration [FA-10] or deceleration [FA-12] time.
- Clean cooling fan/ducts if environment is hot.
|
E006
Braking resistor overload error |
Cause:
- Insufficient deceleration time.
- Load inertia is large or capacity of braking resistor is small.
- Continuous regenerative operation or external force rotating the motor.
Remedy:
- Set longer deceleration time in [FA-12].
- Re-examine choice of resistor capacity.
- Reduce repetition cycle of operation.
|
E007
Overvoltage error |
Cause:
- Power supply voltage fluctuation.
- Large load inertia causing high regenerative power.
- Motor rotated by external force (fan, crane).
- Mutual interference from two inverters on the same shaft.
Remedy:
- Check power supply; consider AC reactor.
- Enable overvoltage suppression [bA140]/[bA146].
- Use a braking resistor, braking unit, or regenerative converter.
- Increase deceleration time [FA-12].
|
E008
Memory error |
Cause:
- Noise interference.
- Power-off occurred during memory access.
Remedy:
- Install noise shielding plates.
- Restore data from keypad backup or initialize inverter.
- If initialization fails, repair is required.
|
E009
Undervoltage error |
Cause:
- Power supply voltage decreased or power failure.
- PS capacity insufficient.
- Contact fault in circuit breaker.
- Capacitor deterioration or circuit failure.
Remedy:
- Re-examine power supply environment.
- Use retry function if failure was temporary.
- Check magnetic contactor/breaker. Repair if necessary.
|
E010
Current detector error |
Cause:
- Current detector circuit is broken.
- Noise source is nearby.
Remedy:
- If error recurs after reset, repair is required.
- Implement noise countermeasures (shielding).
|
E011
CPU error |
Cause:
- Internal CPU malfunction.
- Noise source nearby.
- Data inconsistency during writing.
Remedy:
- Reset, power cycle, or initialize the inverter.
- If no recovery, CPU is broken (repair required).
- Use shielding plates against noise.
|
E012
External trip error |
Cause:
- External device triggered the trip signal.
- Terminal logic reversed or wiring wrong.
Remedy:
- Check external device status.
- Verify input terminal assignment and A/B contact settings.
|
E013
USP error |
Cause:
- Operation command entered immediately upon power ON (within 1-2 seconds).
- Operation command was not released before power ON.
Remedy:
- Wait 2 seconds or longer after power ON to enter operation command.
- Release operation command (switch off) before turning on power.
|
E014
Ground fault error |
Cause:
- Ground fault in wires or motor.
- Motor insulation deterioration.
Remedy:
- Turn OFF power. Disconnect motor wires. Check motor/wires.
- Do not turn ON power while ground fault exists.
|
E015
Incoming overvoltage error |
Cause:
- Incoming voltage is too high.
- Power supply has become unstable.
Remedy:
- Re-examine power supply environment.
- Check for facility replacements causing voltage changes.
|
E016
Instantaneous power failure error |
Cause:
- PS voltage decreased due to power failure.
- Contact fault in circuit breaker.
Remedy:
- Check power supply capacity.
- Check magnetic contactor/breaker.
|
E019
Temperature detector error |
Cause:
- Temperature detector circuit disconnected or broken.
Remedy:
- Repair is required (circuit broken).
|
E020
Cooling fan rotation speed reduction error |
Cause:
- Foreign object stuck in fan.
- Fan end of life.
Remedy:
- Remove foreign object.
- Replace cooling fan.
|
E021
Temperature error |
Cause:
- High carrier frequency.
- Clogged heatsink fins.
- High ambient temperature or poor ventilation.
- Improper installation.
Remedy:
- Lower carrier frequency setting.
- Clean the fins.
- Improve cooling environment.
- Install according to manual.
|
E024
Input open-phase error |
Cause:
- Input line/motor loose connection.
- Single-phase input used on 3-phase setting.
Remedy:
- Check input lines and breaker terminals. Tighten screws.
- Use three-phase connection.
|
E030
IGBT error |
Cause:
- Ground fault, short circuit, or output element failure.
- Motor rotation locked.
Remedy:
- Disconnect motor and check wires/insulation.
- Remove cause of motor lock.
- If element broken, repair required.
|
E034
Output open-phase error |
Cause:
- Output line/motor loose connection or disconnected.
- Motor insulation breakdown.
Remedy:
- Check output wiring and motor condition.
- Re-tighten screws.
|
E035
Thermistor error |
Cause:
- Motor overheated (cooling insufficient or heavy load).
- Inadequate thermistor setting.
- Thermistor broken or noise interference.
Remedy:
- Improve cooling or reduce load.
- Check thermistor settings and wiring.
- Separate wiring to reduce noise.
|
E036
Brake error |
Cause:
- Disconnection of brake check signal line.
- Brake function setting (timing/logic) incorrect.
Remedy:
- Check signal wiring.
- Re-examine brake check waiting time and logic.
|
E038
Low-speed range overload error |
Cause:
- Motor load is heavy at low frequency (0.2Hz or below).
Remedy:
- Reduce load at low-speed range.
- Select larger capacity inverter if frequent.
|
E039
Controller (inverter) overload error |
Cause:
- Operation under heavy load continued.
- Insufficient acceleration torque.
- Load inertia is large.
Remedy:
- Check load condition.
- Adjust boost function [Hb141] or control method.
- Increase accel/decel time.
|
E040
Operator keypad communication error |
Cause:
- Loose connection/disconnection.
- Noise interference.
Remedy:
- Check wiring/connection.
- Take noise countermeasures (wiring separation).
|
E041
RS485 communication error |
Cause:
- Loose connection/disconnection.
- Noise interference.
Remedy:
- Check wiring.
- Take noise countermeasures.
|
E042
RTC error |
Cause:
Remedy:
- Replace battery and set date.
|
E043
EzSQ illegal instruction error |
Cause:
- Program not entered or writing error due to noise.
Remedy:
- Write program after initialization.
- Avoid noise during writing.
|
E044
EzSQ nest count error |
Cause:
- Program structure too complicated (nesting > 8 times).
Remedy:
- Improve program structure.
|
E045
EzSQ executive instruction error |
Cause:
- Program flow inadequate (invalid “for/next/goto”).
- Math overflow/underflow/div by zero.
- Non-existing parameter accessed.
Remedy:
- Check program logic and arithmetic operations.
- Check parameter instructions.
|
E050 to E059
EzSQ user-assigned errors |
Cause:
- Program triggered a user-assigned error instruction.
Remedy:
- Check content of trip instruction in EzSQ program.
|
E060 to E089
Option 1/2/3 errors |
Cause:
- Option not securely mounted.
- Option used incorrectly.
Remedy:
- Check option mounting.
- Refer to specific option manual.
|
E090 to E096
STO path / FS option error |
Cause:
- Safety function system has problems.
Remedy:
- Refer to “Functional Safety Guide”.
|
E100
Encoder disconnection error |
Cause:
Remedy:
- Refer to P1-FB user’s guide.
|
E104
Position control range error |
Cause:
- Position counter exceeded range.
- Improper electronic gear or encoder setting.
- Slipping due to mounting.
Remedy:
- Recheck electronic gear/encoder settings.
- Check encoder mounting.
|
E105
Speed deviation error |
Cause:
- Deviation between frequency command and feedback speed.
- Improper encoder/gear setting.
Remedy:
- Re-examine load conditions.
- Check encoder/gear settings.
|
E106
Position deviation error |
Cause:
- Position feedback deviation exceeds limit.
Remedy:
- Re-examine load conditions.
- Check encoder/gear settings.
|
E107
Over-speed error |
Cause:
- Speed exceeded detection level.
Remedy:
- Re-examine operation/load conditions.
- Check encoder/gear settings.
|
E110
Contactor error |
Cause:
- Wiring defect in intelligent input.
- Contactor response defect.
Remedy:
- Check setting and wiring of intelligent input.
- Check contactor operation and response time.
|
E112
Feedback option connection error |
Cause:
- Connection error related to feedback options.
Remedy:
- Refer to P1-FB user’s guide.
|